944T project updates
Posted: Tue Jun 10, 2025 5:57 am
Hello all -
Finally back to the car. Some Updates and time to get back to work on this car.
So...since my last threads here is where we are:
1. When I paused working it was due to a small fire! The fuel line at the FPR sprung a leak and must have been ignited by the burning insulation on the O2 sensor wiring that got too close to the turbo inlet feed...no major damage other than scorching the paint on the hood which will now have to be repainted. UGH but could have been much much worse!
2. Had to rewire some things and move the harness around a bit to alleviate concerns. All in all it was a good thing as I believe everything is much better positioned and secured better than in version one
3. Car is back to running now!
3. Still fighting two oil leaks...I finally had a chance to get the car on my buddy David's lift to really figure out what is going on. We pulled the transmission (good because it needed to be cleaned and I added some reinforcement to the trans bracket to reduce the sway) and exhaust so I could see where the rear leak was coming from. Oil pan seal looked good and after the dye we could easily see the Rear Main Seal must have torn or something. Replaced that and no more leak there. The other leak is in the front of the engine. In my other posts related to this - I was looking at the lower balance shaft. Oil drips down right at the corner of the oil pan where it makes the soft 90 degree turn towards the oil pump. We were able to slowly remove the bal shaft carrier to determine that the seal is working great up until it comes out of the shaft housing, so we know that is sealing correctly. No oil out of the front seal. So we are back to the oil pump not seating properly. Pump has been removed and all of my stop gap Yamabond removed/cleaned up so we can really fix the issue. It looks like there is in fact a little area about where the leak was where not enough Locktite 574 was on the sealing surface and this could have been the problem. Will clean these surfaces good and then reassemble. Hopefully this will take care of the leaks.
4. In the spirit of making improvements to the first version of the install (remember I am going to a microsquirt here), I am looking again at the setup of my trigger wheel on the front crank pulley sandwich. Everything works fine in this situation, but I was concerned at the initial lack of oil pressure perhaps from the crank bolt not tightening enough to turn the pump drive gear. I added a washer between the bottom of the PS pulley around the crank to give me an extra 2mm or so of depth to compensate for the depth of the trigger wheel and ensure the convex washer had enough to pull against before the crank bolt bottomed out. My question is do I really need that washer, and is the threaded portion of the inside of the crank actually longer than the threaded part of the bolt such that there is room for it to tighten down enough without the washer? Again - everything works fine, but I am trying to make improvements and the extra washer is just one extra part in there.
So thoughts on this long email - I am glad to just have this project slowly moving forward again.
Finally back to the car. Some Updates and time to get back to work on this car.
So...since my last threads here is where we are:
1. When I paused working it was due to a small fire! The fuel line at the FPR sprung a leak and must have been ignited by the burning insulation on the O2 sensor wiring that got too close to the turbo inlet feed...no major damage other than scorching the paint on the hood which will now have to be repainted. UGH but could have been much much worse!
2. Had to rewire some things and move the harness around a bit to alleviate concerns. All in all it was a good thing as I believe everything is much better positioned and secured better than in version one
3. Car is back to running now!
3. Still fighting two oil leaks...I finally had a chance to get the car on my buddy David's lift to really figure out what is going on. We pulled the transmission (good because it needed to be cleaned and I added some reinforcement to the trans bracket to reduce the sway) and exhaust so I could see where the rear leak was coming from. Oil pan seal looked good and after the dye we could easily see the Rear Main Seal must have torn or something. Replaced that and no more leak there. The other leak is in the front of the engine. In my other posts related to this - I was looking at the lower balance shaft. Oil drips down right at the corner of the oil pan where it makes the soft 90 degree turn towards the oil pump. We were able to slowly remove the bal shaft carrier to determine that the seal is working great up until it comes out of the shaft housing, so we know that is sealing correctly. No oil out of the front seal. So we are back to the oil pump not seating properly. Pump has been removed and all of my stop gap Yamabond removed/cleaned up so we can really fix the issue. It looks like there is in fact a little area about where the leak was where not enough Locktite 574 was on the sealing surface and this could have been the problem. Will clean these surfaces good and then reassemble. Hopefully this will take care of the leaks.
4. In the spirit of making improvements to the first version of the install (remember I am going to a microsquirt here), I am looking again at the setup of my trigger wheel on the front crank pulley sandwich. Everything works fine in this situation, but I was concerned at the initial lack of oil pressure perhaps from the crank bolt not tightening enough to turn the pump drive gear. I added a washer between the bottom of the PS pulley around the crank to give me an extra 2mm or so of depth to compensate for the depth of the trigger wheel and ensure the convex washer had enough to pull against before the crank bolt bottomed out. My question is do I really need that washer, and is the threaded portion of the inside of the crank actually longer than the threaded part of the bolt such that there is room for it to tighten down enough without the washer? Again - everything works fine, but I am trying to make improvements and the extra washer is just one extra part in there.
So thoughts on this long email - I am glad to just have this project slowly moving forward again.