89 951 engine overhaul
Posted: Mon Apr 11, 2022 11:44 pm
Well, it's long past due I stuff all this into a thread of my own. I've certainly gotten a lot out of others' threads like this, so I'll try and document some of what I come across...Maybe even ask some questions along the way 
I planned to pull my engine over the winter - it's been out for, oh, most of a month (by April). Nothing huge, just one too many dry seals and enough crud built up that I went for it.
todo list now looks something like this:
Out! Mounted: My janky RTV balance shaft repair seems in decent shape:
I've only pulled the #2 bearing, here's what that looks like: And on the reverse (side in compression/rod side): I'm an amateur, but this looks shockingly good. Maybe less the marring on the thrust side...not sure what to make of that!
Finally, ....A surprise washer:
Findings so far:
- Cast rods
- I forgot to do a leakdown test again - #3 had high (15%?) leakdown before I pulled the motor. Looking at the bores, probably a valve?
- oil pan baffled is cracked up, so going to need to find a new one.
Bores are here, I don't need 8 images in-line!
I planned to pull my engine over the winter - it's been out for, oh, most of a month (by April). Nothing huge, just one too many dry seals and enough crud built up that I went for it.
todo list now looks something like this:
- M030 front strut refurb
- Turbo refurb (K26/8 hybrid from Evergreen)
- Tial 38mm
- Rod bearings (ACL)
- Forged rods...
- Rings?
- Every damn seal
- Clutch (930? Cup?), PP (KEP1), associated bearings
- Oil cooler and lines
- VEMS plug-and-play
- Steering rack reseal
- Control arms
- Tie rods
- Head refresh (has new springs, plus MM's "insurance" inners)
- Voith's balance shaft rear seals
- Window seals on both doors (completely dryrotted, scratched the windows!)
Out! Mounted: My janky RTV balance shaft repair seems in decent shape:
I've only pulled the #2 bearing, here's what that looks like: And on the reverse (side in compression/rod side): I'm an amateur, but this looks shockingly good. Maybe less the marring on the thrust side...not sure what to make of that!
Finally, ....A surprise washer:
Findings so far:
- Cast rods
- I forgot to do a leakdown test again - #3 had high (15%?) leakdown before I pulled the motor. Looking at the bores, probably a valve?
- oil pan baffled is cracked up, so going to need to find a new one.
Bores are here, I don't need 8 images in-line!